At the behest of Würger, and to save from completely hi-jacking Evan's "Braun-Vier" thread, I shall continue my mad ramblings here... The point we're upto (for those who havent noticed the last posts in the aforementioned thread) is that I am experimenting with PE, in order to create accurate Engine Mounting Arms - previous PE experience has been limited to knocking up PCB's, so going from boards to parts is actually proving more of a leap than expected!
So... on with the show... This is what we're trying to make:
The current (new) acetate that I have is just not doing the trick - I tried three times, with gradually better results, but it was wearing on my patience. I have some idea's on how to improve things, but I'm here to MAKE parts i need NOW; not experiment! The removal of the acetate was shocking the toner after transfer - so making a fast quench in water when its hot, or removal of the acetate while things are still hot would be a better plan, but we'll worry about that later.
... see; and while that MIGHT work (there is still toner down in the 'light areas'), I just dont want to be playing with maybe's...
BUT, when digging up some degreaser and chemical cleaner, I happened up a few sheets of Press-n-Peel, for printing PCB's; thus I thought I may as well try them. Print out, line up ( SOOOOO much harder through a mostly opaque sheet!!!!), iron on to CLEANED Brass... Not perfect, but we at least now have something to play with:
As you see, there a few little issues; minor surface contaminant in one spot (probably dust or something between the brass and toner) and the odd lift mark where insufficient heat was used, but on the whole, it will do. You'll notice that small issues can be corrected with either some ordinary modelling paint or with a permanent marker or anything that will form a barrier between the etchant and the metal.
The next step is to mix up a small batch of etchant (Ammonium Persulphate in my case), keep it between 70-80degC and etch the parts for 5-10mins...
Dan
So... on with the show... This is what we're trying to make:
The current (new) acetate that I have is just not doing the trick - I tried three times, with gradually better results, but it was wearing on my patience. I have some idea's on how to improve things, but I'm here to MAKE parts i need NOW; not experiment! The removal of the acetate was shocking the toner after transfer - so making a fast quench in water when its hot, or removal of the acetate while things are still hot would be a better plan, but we'll worry about that later.
... see; and while that MIGHT work (there is still toner down in the 'light areas'), I just dont want to be playing with maybe's...
BUT, when digging up some degreaser and chemical cleaner, I happened up a few sheets of Press-n-Peel, for printing PCB's; thus I thought I may as well try them. Print out, line up ( SOOOOO much harder through a mostly opaque sheet!!!!), iron on to CLEANED Brass... Not perfect, but we at least now have something to play with:
As you see, there a few little issues; minor surface contaminant in one spot (probably dust or something between the brass and toner) and the odd lift mark where insufficient heat was used, but on the whole, it will do. You'll notice that small issues can be corrected with either some ordinary modelling paint or with a permanent marker or anything that will form a barrier between the etchant and the metal.
The next step is to mix up a small batch of etchant (Ammonium Persulphate in my case), keep it between 70-80degC and etch the parts for 5-10mins...
Dan