swampyankee
Chief Master Sergeant
- 4,022
- Jun 25, 2013
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Would a laminar type wing have helped the P-38.
Would a laminar type wing have helped the P-38.
First, laminar flow airfoils of that era, like NACA's 6 series airfoils, could not maintain laminar flow in service (indeed, even today it's considered normal practice to use the lift and drag characteristics with a tripped boundary layer, i.e., one that is turbulent), so there is not likely to be much drag reduction.
However, because some of the 6 series airfoils were designed to have maximum flow velocity (maximum Cp) fairly far aft, they had higher critical Mach numbers than other airfoils.
So, the answer to the question is "maybe yes, maybe no." I'd vote for probably no.
Some caveats are needed here, I think. First is that most of the reviewers are Navy and almost all military pilots are highly bias for one, their aircraft, and two, their service. Second, I am sure all the reviewers were single engine pilots. As such, the plane is big, complex, and they were unfamiliar with two engine idiosyncrasies like, maybe, asymmetric thrust.
Overall, I think the P-38 had potential to be an effective fighter, it was certainly deadly in the PTO. However, I suspect it took some time for a pilot to learn how to handle the uniqueness of the aircraft. Also, two engines adds cost, reduces mission reliability and increases maintainability requirements. Faced with the simplicity, cost, ease of flying and performance of the P-51, it was difficult to justify.
Even with the arrival of the P-38J, engines and turbochargers continued to fail. The new intercooler/oil cooler design was actually too efficient and the enlarged radiators became a new problem. Fuel too, was a source of trouble, it is believed by many knowledgeable people that the majority of fuel used in Britain was improperly blended, the anti-knock lead compounds coming out of solution (separating) in the Allison's induction system at extreme low temperatures. This could lead to detonation and rapid engine failure, especially at the higher power settings demanded for combat.
Many of the P-38's assigned to escort missions were forced to abort and return to base. Most of the aborts were related to engines coming apart in flight. The intercoolers that chilled the fuel/air mixture too much. Radiators that could lower engine temps below normal operating minimums. Oil coolers that could congeal the oil to sludge. These problems could have been fixed at the squadron level. Yet, they were not. It took the P-38J-25-LO and L model to eliminate these headaches. Add sub-standard fuel, green pilots, poor tactics and the 8th had a serious problem in the making.
If you fly a turbocharged engine, you need to know how the system works and be aware of several important operating techniques. Because oil pressure closes the wastegate, you must allow time for the engine and oil to warm up completely before taking off. If the oil pressure is low or the oil is cold and sluggish, the wastegate may be slow to close, which means the engine won't develop its full, rated power during takeoff and climb.
Also, engine oil lubricates the turbocharger, which can spin at more than 30,000 rpm at takeoff power During normal operation, several gallons of oil flow through the turbocharger's bearings every minute. Cold oil doesn't flow properly. If you apply high power settings before the oil warms to the proper temperature, the oil may not lubricate the turbocharger sufficiently.
Power should be applied smoothly and relatively slowly. If the throttle is shoved rapidly to the firewall on takeoff, the turbocharger controlling mechanisms may not have time to function properly, causing the engine to surge and possibly overboost.
Unfortunately P-38 engines required 5 years to fix (1939 to 1944). By then the war was almost over..
Biggest problem when discussing P-38 reliability is that sources disagree. Some claim problems were fixed by 1943. Other sources claim problems were never completely fixed.
However it's a fact that U.S. 8th Air Force chose to replace P-38s with P-47s and P-51s when enough of those fighter types became available. Production cost can't be the issue as P-47 costs almost as much as a P-38. P-47 was also a fuel hog. P-47 and P-51 both had weapon packages inferior to P-38. So I've got to assume people operating P-38s at high altitude lacked confidence in the aircraft even during 1944. I have not personally flown the aircraft and can only defer to those that did historically under combat conditions.
Many pilots disliked the P-47 (i.e. most numerous American fighter aircraft). Especially if they had experience flying other fighter types. So I'm not surprised some expressed a strong preference for the P-38 even if it had technical glitches.
Thanks for the link. Both P-38s were flown without leading edge tanks, and we are left in dark why the P-38K was not faster under ~30000 ft on WEP - it did have 2x1725 HP, vs 2x1600, in the same time featuring a better prop.
tomo pauk said:The weight of 30 gals of ADI liquid (water-methanol) in the P-47 was 124 lbs. Lockheed assumed that ADI system would've weighted 600 lbs, 400 lbs being the ADI liquid - seems they intended to replace the LE fuel tank with ADI tank - 400 lbs is almost 100 gals of water-methanol?
Read the first sentence of the second paragraph. Speed at 1725 hp would have been about 2% better at all altitudes.
The weight of 30 US gallons ADI was about 224-248 lbs. (50-50 to 95-5 water-alcohol) Total system weight for the P-47 was less than 300 lbs.
The P-38 system seems to be a 24x2 gallon system. This system was not where the leading edge tanks were but most likely located in the wheel wells and/or outboard of the nacelles behind the main spar. The fixed weight of the systems seems very high for the capacity.
tomo pauk said:Many thanks for pointing me at power setting used.
If I'm reading the report right, the RoC (all altitudes) and speed (at lest from 35000 up?) was only because a better prop was installed?
tomo pauk said:Thanks again.
I've read the item 'Water' (124 lbs) on the table at pg. 285 of AHT book, and then there is another item named 'Water', on the same table but lower, and this item weights 248 lbs (or zero lbs for 'Design' mission profile). Anyone up to clear it to me why two items of same name are listed there - 248 lbs would indeed be the ADI liquid.
tomo pauk said:I'd love to see a proper description of the system myself; the 2 x 24 gall system does make much more sense. BTW, if the ADI tank is located behind the main spar, it might cut into the inboard (main) fuel tank, or may dictate different construction/location of the dive flaps.
The paragraph 5 from the linked document says that Lockheed assessed that weight penalty will be 600 lbs for the ADI system, out of which 400 lbs is to be water(/methanol).
The top part of the table is for early models with the 15 gallon tank and the bottom is for later models with the 30 gallon tank.
Nothing in the report suggests that the normal fuel capacity was reduced in any way.
My best guess is the system had two 12 gallon tanks per engine located in side the main wheel wells just in front of the supercharger intakes.