1:48 Engine Room #3 Battleship USS New Jersey for Permanent Display on Board.

Ad: This forum contains affiliate links to products on Amazon and eBay. More information in Terms and rules

Thanks guys! The new printer is astounding in both it's resolution and producing parts without any failures. And of course, the paint's barely dry on this one and Elegoo is now marketing the Saturn 4 Ultra 16k. Mine has a 12k LCD screen, so the new one has a 30% resolution. I don't know what that means, but in the case of the my Saturn, the increase from 4k in my Mars 3 to 12k in the Saturn has made a huge difference in apparent performance. I used "apparent" becuase of the increase area of the larger build plate decreases the absolute increase in pixels per unit area, Regardless, it is a higher resolution machine. Since the new Saturn model has the same size build plate, it's pixel pre unit area is increased proportionately.

I'm producing one to two runs per day. Today, I cleaned up the full reduction gear sets and started printing the HP turbine in all its entirety. It will be done at 6:30 p.m. so I'll know if its a good print tonight. I've come to expect that all the prints are going to be good. I only had a single failure since I got this machine, and that was very early on. The more accurate exposure time and the resolution making much higher strength parts enables me to use medium supports throughout the part except for the starting surfaces at the build plate. This makes support removal much easier since the medium (and fine) supports pull off by hand and leave no nibs behind.

To give you all a reference of just how massive a 53, 000 hp gear box is, here's the bull gear with a scale person next to it.

NJ ERP Bull Gear is Huge.jpg


The Gear sets are really nice. I knew in the drawing that one set was not in direct, tight contact with the input pinion and suspected that when supports were removed, it would be a separate part. It is! Not a problem since it will settle into it's bearing mounts and will look fine. Here's how they looked coming out of the machine.

NJ ERP Reduction Sets as Printed.jpg


And again, with our scale 1:48 man. There are some very minor blemishes in the gear teeth, but I'm totally okay with that and am pleased with the outcome.

NJ ERP Reduction Sets Preped.jpg


Another view… I made the shafts hollow to reduce resin consumption.

NJ ERP Reduction Sets.jpg


I have all the propulsion system parts loaded (by WiFi) in the printer, so all I have to is pull the job off, fill up the vat to account for resin consumption, press go and in a few hours more parts will appear. Here's what it looks like in time lapse from the printer's build in camera. It's fascinating and a little sci-fi to have parts appearing of a 1/2" deep pool of resin.




Hope the video works….
 
Thanks guys! The new printer is astounding in both it's resolution and producing parts without any failures. And of course, the paint's barely dry on this one and Elegoo is now marketing the Saturn 4 Ultra 16k. Mine has a 12k LCD screen, so the new one has a 30% resolution. I don't know what that means, but in the case of the my Saturn, the increase from 4k in my Mars 3 to 12k in the Saturn has made a huge difference in apparent performance. I used "apparent" becuase of the increase area of the larger build plate decreases the absolute increase in pixels per unit area, Regardless, it is a higher resolution machine. Since the new Saturn model has the same size build plate, it's pixel pre unit area is increased proportionately.

I'm producing one to two runs per day. Today, I cleaned up the full reduction gear sets and started printing the HP turbine in all its entirety. It will be done at 6:30 p.m. so I'll know if its a good print tonight. I've come to expect that all the prints are going to be good. I only had a single failure since I got this machine, and that was very early on. The more accurate exposure time and the resolution making much higher strength parts enables me to use medium supports throughout the part except for the starting surfaces at the build plate. This makes support removal much easier since the medium (and fine) supports pull off by hand and leave no nibs behind.

To give you all a reference of just how massive a 53, 000 hp gear box is, here's the bull gear with a scale person next to it.

View attachment 815158


The Gear sets are really nice. I knew in the drawing that one set was not in direct, tight contact with the input pinion and suspected that when supports were removed, it would be a separate part. It is! Not a problem since it will settle into it's bearing mounts and will look fine. Here's how they looked coming out of the machine.

View attachment 815159

And again, with our scale 1:48 man. There are some very minor blemishes in the gear teeth, but I'm totally okay with that and am pleased with the outcome.

View attachment 815160

Another view… I made the shafts hollow to reduce resin consumption.

View attachment 815161

I have all the propulsion system parts loaded (by WiFi) in the printer, so all I have to is pull the job off, fill up the vat to account for resin consumption, press go and in a few hours more parts will appear. Here's what it looks like in time lapse from the printer's build in camera. It's fascinating and a little sci-fi to have parts appearing of a 1/2" deep pool of resin.


View attachment 815162

Hope the video works….
🥓

The figure really adds scale to the work. It's pretty neat!
 
The HP print looks spectacular!

NJ ERP HP Parts as printed.jpg


Even that very complex throttle assembly printed perfectly and I left it attached to the upper half.

NJ ERP Throttle CU Before Trim.jpg


I didn't know if it would work that way. It did!

NJ ERP HP Rotor Discharge End.jpg


The rotor is a beauty with no warpage and clearly define discharge-end blading.

NJ ERP HP Rotor no Warp.jpg
And that very thin cross-section exhaust funnel seems to be okay too.

NJ ERP Exhaust Funnel Success.jpg


Lower shell is nice and clean and should work as drawn.

NJ ERP HP Lower Housing.jpg


I haven't trimmed it or post-cured it so things can still break.
 
The printer continues to hum along turning out very nice parts. I test assembled the HP turbine. The rotor broke in the middle. I temporarily glued it back together, but am reprinting another. It appeared to be a structural flaw, and after reviewing the drawing, there were some discontinuities in the central core. I made some mods and in the slicer it appears to be nicely solid all the way through. It's set up to print with the main steam pipe. The rest of the turbine came out great with no changes necessary. My removal of the supports left all the throttles in good shape. Just finished on the machine is the entire HP foundation frame printed as a single part and it's appears to be perfect. I also printed the "steel" stiffener that resides on the fire room side of that bulkhead that provides the necessary to support the ledge on which 1/2 of the turbine rests. I have that part to display tomorrow.

NJ ERP HP Test Assembly.jpg


The massive lower half of the main reduction gear box is done. As the rest of this work, this one was very nice also.
NJ ERP MRG Base in Printer 2.jpg
NJ ERP MRG Base in Printer.jpg


This part consumed a lot of resin! It supports the output shaft from the bull gear.
NJ ERP MRG Based Prepped.jpg


Looking at it from the bottom shows the lower half of the output seal and bearing.

NJ ERP Output Flange.jpg


This picture is a bill silly since there's no shaft supporting the big gear, but this shows where it resides and why the gear case is do darn big.

NJ ERP MRG Where the Bull Gear Goes.jpg


Creating a model of this complexity and novelty is like the aphoism about how to eat an elephant; "One bite a time." With each successful drawing and subsequent print, I am more sure that the project will meet my goals. And I've said this before. When doing a completely custom build, you're thinking on a few levels at the same time. It's very easy to get the forrest and the tree, or roots, moss, fungus…etc. It's so easy to get down to very tiny details before you have control of the overall design and how it will work together. I can just imagine putting a show together like Game of Thrones (GOT). My wife finally agreed to watch it. I saw it when it first ran years ago. When you look at the scope of the script, the locations it was shot at, the costuming, sets, and then the cinematography, you wonder how they do it at all. Each episode was like a 1st run movie. My project IS NOT that.

My daughter's, brother in law's brother is one of the two fellows who created GoT, D.B. Weiss. We had the pleasure of visiting D.B.'s family home in a Chicago suburb. We talked at length about the creation of the show. It turns out that a pilot was created, but it was terrible and HBO didn't want anything to do with it. Dan and David told Netflix that wanted to rewrite and produce the pilot. No one bit, but the president decided to give it a shot. The rest is history. Netflix made billions on that show over its 8-year run and the two fellows didn't do so bad either. It just shows that sometimes even folks that are supposed to know, do know nothing. His mom presented us the full 8 year set on Blue Ray DVDs. We fianlly are watching it.
 
Moving along…The HP Foundation/frame printed exceedingly well. No layer marks, perfect holes and no warp. It's all cleaned, but not post-cured. The upper beam ends in that bracketed shelf. The other part is the stiffening structure on the other side of the bulkhead that strengthens the whole deal. It's also part of the boiler support system.

NJ ERP HP Foundation.jpg
NJ ERP HP Foundation top.jpg

My spouse has a strictly enforced rule… "No shop work after 5pm and no shop work on the weekends". Considering how much treasure and time my "shop work" consumes, I abide by these rules without exception.

The printer has another feature. It expects that the PAF Teflon seal film on the vat bottom to last 60,000 layers. When it hits 60,000, the printer stops and issues a warning on the touch screen which you can override. I overrode it for one print yesterday afternoon and noticed some delamination of the base raft, but it did not affect the print. Turns out that print was unnecessary as it was an out-of-date version of a part which I had already printed the day before. So the delamination didn't matter. Last night's part did. It was the top half of the gear box and the corrected diameter of the output shaft. It was a failure. The film is shot and needs to be replaced. From now on, I will heed the machines warning. It knows better than me. Just for the record. I printed those 60,000 layers with no failures until this one.

This part is NOT salvagable. However, on the other end of the print (not shown) is a correct diameter output shaft and it is usable as are the torque tube shields for the LP and HP output shafts. So it's not a total loss. On Monday, my first assignment will be to replace the PAF. I bought extra film when I bought the printer. In the past, you just tracked how many failures and when they seemed chronic, you changed the film.

NJ ERP 60000 fallure.jpg


I finalized the condensate pump system and exported its STL file. I sliced it and WiFied it to printer. All of the parts of the primary propulsion system are either printed or in the printer's local memory and will be printed this coming week. I'm printing it with the piping. The printer's precise enough to pull that off, especially since i did it with my older printer on the ammo hoists on the 5" project and they came out okay. The dark openning in the top is the steam inlet. There's another around the side for exhaust. These will be piped.


Condensate Pump.png
 

Users who are viewing this thread

Back