drgondog
Major
Well as you know at close to Mach 1 even small defeciencies can be fatal. Lets say a panel comes off at Mach 0.85 because of a small gap made in assembly, well that could cause the whole a/c to come apart.
If you think a 1/4" gap between butt joint panels would make a difference at Mach 1, much less Mach 2 - you have never seena Mig 21 up close. 'gap's might make a difference in drag if those panels were immersed in a boundary layer but you wouldn't notice it in turbulent region.
Wrong argument.
The pace at which a/c were being contructed in 1945 as well as, and no less, the circumstances under which they were made, enevitably caused a lot of quality issues. But to make matters even worse the LW, in order to get enough a/c in the air, had to significantly lower their quality acceptance demands. Hans Fey also notes the lower quality acceptance demands and differing workmanship between a/c in the report on the site I referenced earlier.
The only 'quality issues' that would make a lot of sense would be heat treat/metullurgy issues on High strength fastners and casting/forgings. You have any data showing those were the issues of concern?
Infact by 1945 Hungarian built 109's were considered to be of much better quality than German built ones.
You said earlier that 'only a few' 262s exhibited a tendency to hunt' - which is at variance with all the 262s tested by USAAF after the war. You stated those were 'quality issues'?? also. With respect to what?
Yes, but will it stay together ?
That HAS been the question Soren with zero substantiation that yes, the me 262 as designed and built, will in fact take the aerodynamic loads associated with .89- 1.0 Mach..
and that the pitch down issue at .83 to .86 was somehow solved, that the associated bending and torsion forces that would be experienced attempting to control high speed yaw (on Rudder) and pitch (slab tail with very high associated stick forces) were 'not a problem' and shown to be so with rigorous stability and control analysis coupled with professional aero analysis and advanced structural solutions taking all that into account..
Why isn't the logic and fact base so compelling that anyone (not even Everyone) agrees with you.. Messerschmidt didn't, the RAF and USAAF Test pilots didn't, I have seen zero LW Test pilots giving testimony in 1944-1945 when they were actually flown, the Russians quit flying it past .86 after barely surviving the experience, the Czechs (to my knowledge) never pushed it past .84. THERE is a HUGE drag rise between .82 and .9 - much less 1.0 assuming stability and control issues were ever solved.
The modern day builders (Stormbird) placard the airframe at 540kts at SL (~.82M) despite a far superior engine, improved internal structure and internal/extenal quality. Why?
You think you have made your speculative case?